This seems to be running alittle slow in my opinion. It's powdered by a futaba s3003 servo motor which should run at 4.8V: 0.23 sec/60° 6.0V: 0.19 sec/60. It's powered from the 5v flasher circuit which was originally inside the dalek topper. Now I've countersunk all the screws and there's nothing catching so I'm assuming there's not enough power to the servo to meet it's full potential?
I've read all the posts on pinside and done all the googling. It's not affected when you unplug the GI.
Just wondered if there's any of you clever clogs out there that could point in me in the right direction.
There's plenty of videos on youtube and all of those run far faster than this. I'm stumped
Original instructions
http://www.instructables.com/id/Motorizing-the-Doctor-Who-Pinball-Dalek/?ALLSTEPS
Cheers
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